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usb: musb: fix pm_runtime mismatch

In musb_init_controller() there's a pm_runtime_put(), but there's no
pm_runtime_get(), which creates a mismatch that causes the driver to
sleep when it shouldn't.

This was introduced in 7acc619[1], but it wasn't triggered in my setup
until 18a2689[2] was merged to Linus' branch at point df0914[3]. IOW;
when PM is working as it was supposed to.

However, it seems most of the time this is used in a way that keeps the
counter above 0, so nobody noticed. Also, it seems to depend on the
configuration used in versions before 3.1, but not later (or in it).

I found the problem by loading isp1704_charger before any usb gadgets:
http://article.gmane.org/gmane.linux.kernel/1226122

All versions after 2.6.39 are affected.

[1] usb: musb: Idle path retention and offmode support for OMAP3
[2] OMAP2+: musb: hwmod adaptation for musb registration
[3] Merge branch 'omap-for-linus' of git://git.kernel.org/pub/scm/linux/kernel/git/tmlind/linux-omap-2.6

Cc: stable@vger.kernel.org
Cc: Hema HK <hemahk@ti.com>
Signed-off-by: Felipe Contreras <felipe.contreras@gmail.com>
Signed-off-by: Felipe Balbi <balbi@ti.com>
hifive-unleashed-5.1
Felipe Contreras 2011-12-19 22:01:54 +02:00 committed by Felipe Balbi
parent e7f4e73287
commit 772aed45b6
1 changed files with 0 additions and 2 deletions

View File

@ -2013,8 +2013,6 @@ musb_init_controller(struct device *dev, int nIrq, void __iomem *ctrl)
if (status < 0)
goto fail3;
pm_runtime_put(musb->controller);
status = musb_init_debugfs(musb);
if (status < 0)
goto fail4;