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Input: goodix - disable IRQs while suspended

[ Upstream commit faec44b683 ]

We should not try to do any i2c transfers before the controller is
resumed (which happens before our resume method gets called).

So we need to disable our IRQ while suspended to enforce this. The
code paths for devices with GPIOs for the int and reset pins already
disable the IRQ the through goodix_free_irq().

This commit also disables the IRQ while suspended for devices without
GPIOs for the int and reset pins.

This fixes the i2c bus sometimes getting stuck after a suspend/resume
causing the touchscreen to sometimes not work after a suspend/resume.
This has been tested on a GPD pocked device.

BugLink: https://github.com/nexus511/gpd-ubuntu-packages/issues/10
BugLink: https://www.reddit.com/r/GPDPocket/comments/7niut2/fix_for_broken_touch_after_resume_all_linux/
Tested-by: Hans de Goede <hdegoede@redhat.com>
Signed-off-by: Hans de Goede <hdegoede@redhat.com>
Reviewed-by: Bastien Nocera <hadess@hadess.net>
Signed-off-by: Dmitry Torokhov <dmitry.torokhov@gmail.com>
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
pull/10/head
Hans de Goede 2018-01-12 00:36:48 -08:00 committed by Greg Kroah-Hartman
parent c427d7e44a
commit 88f6f0490f
1 changed files with 6 additions and 2 deletions

View File

@ -808,8 +808,10 @@ static int __maybe_unused goodix_suspend(struct device *dev)
int error;
/* We need gpio pins to suspend/resume */
if (!ts->gpiod_int || !ts->gpiod_rst)
if (!ts->gpiod_int || !ts->gpiod_rst) {
disable_irq(client->irq);
return 0;
}
wait_for_completion(&ts->firmware_loading_complete);
@ -849,8 +851,10 @@ static int __maybe_unused goodix_resume(struct device *dev)
struct goodix_ts_data *ts = i2c_get_clientdata(client);
int error;
if (!ts->gpiod_int || !ts->gpiod_rst)
if (!ts->gpiod_int || !ts->gpiod_rst) {
enable_irq(client->irq);
return 0;
}
/*
* Exit sleep mode by outputting HIGH level to INT pin